We had the boat all ready for the rather early 7:30 am relaunch. We even got ourselves there nice and early to pop into the office to ask about where they wanted us to berth. Only that was a waste of time as the berthing master on duty said that there were no spaces free yet, thanks to the Motor Yacht show that had finished the day before. We reminded him that we were booked in by Maricom, a commercial tenant and he looked a bit sheepish.....
Meanwhile, the boat was hanging in slings ready to drop into the water, half an hour early. So the pressure was on - he told us to just stop on the fuel pontoon, which is the one that runs up to the lift bay and that they would call us when they had a space. OK. We rushed to the lift bay, climbed on board and were dropped into the water.
Getting the boat ready to move involved removing the pins from the stabiliser fins to set them free, checking for any water ingress and then firing up the main engine. When the stabiliser control panel was fired up, it made a tortured beeping sound. That was not good. Rebooted, it did the same, with a screen display that looked more like a fish finder than anything to control the stabiliser settings. A third reboot and it did the same, finally coming up with a comms error. Wonderful. The Golden Arrow guys had to plug a sensor into the control box to realign the fin sensors after the bearings were replaced but this made no sense. As there was nothing to do, we had to leave the fins floating free which makes boat manoeuvring highly amusing as you have two big rudder like things that just move in the water flow past the hull and can turn you, act as brakes etc, Wonderful.
The captain headed to the flybridge for the best view and saw a RIB astern of us that we would have to shimmy round. We gently reversed out of the bay and the idea was a little squirt on the stern thruster to kick the stern out so we could back past the moored RIB. Hitting the thruster control the crew who was in the aft cockpit heard a tortured squeal. There was no thrust.... So, a kick ahead to push the stern out with the rudder hard over and a little bit of bow thrust to stop the bow from swinging into the walls of the hoist dock. Then a very slow reverse past the RIB and onto the pontoon.
Tied up we took stock. Stabilisers that would not work and a dead stern thruster. Bad words were said. But why? Surely we cannot have picked up some debris in the hoist bay after relaunch that jammed the thruster? That would be so unlucky. The stabiliser issue was well above our pay grade so a depressed captain and crew pinged a note to the TRAC engineer that had reset the fin sensor position for us. Meanwhile, the captain had a good look at the thruster controls and power supply. This is the cut off button:
A big thing fitted in the lazarette. The Maricom guys had removed the cover to change the wiring around for the new battery to battery charger that would look after the thruster batteries. It seemed that when the cover was refitted it managed to hold the button in a half on, half off position. Wonderful. A couple of on/off movements and the thruster was back to being happy again. One problem down.
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Thanks for your ideas / cheek / corrections / whatever! They should hit the blog shortly after the system checks them to make sure they will not put us or you in jail.....